The cover works awesome!! Lots of heavy rain last week and no pooling and carpet was dry!
I am still frustrated so going with condensed version.
I started unhooking the REgulator and noticed two of its wires were melted together... Damn these barrell connectors suck!
I hooked up the new Regulator first since it was the easiest. Still won't fire. AFter 3 hours I got the Stator replaced air impact is a must for removing the flywheel!!! and a ratchet strap around the flywheel to keep it from spinning. We even had to use the impact on the puller bolt.... I was very careful on this one to make sure nothing was bending etc... ONce stator replaced still wouldn't fire! I spent the next hour looking for any disconnected wires and wouldn't you know I found one unhooked. Still wouldn't start... At this point started looking at the console wiring and damn two wires hanging from the ignition switch... I know I unhooked them all without labeling!!! I go over to the old console and look at the where they could have been hooked up. Well there is no kill switch on this model but at the very bottom corner of the controller hidden by the throttle is an off\run switch....Really 4 years and I had never seen this before! I got it pulled from the old controller and wired to ignition switch. Still wouldn't start. Went over to my Bro's place just pissed. Sent my SIL to get me some brews and my bro came back with me and said smells like massive gas have you cleaned the plugs??? So we clean the plugs let them dry and she fires up!! Put it on the hose and she ran like a champ for 15 minutes. Forward, reverse, fast throttle, slow throttle, Tilt works great alright! I call the admiral to make the call to everyone She is running come on down for the weekend. I turned it off and decided to figure out why the tach has been reading 7k from the time I hooked up the console on the boat. I look for loose wires at the tach and couldn't find any. Try to start it and nothing. After 30 minutes ignition switch won't do anything not even a click. I make the call to tell everyone forget about the weekend. The tilt and trim gets its power from the ig switch and now it doesn't work. It will if I bypass the hot with an accessory wire.. I use my dc tester and all the hot wires to switch now read ground and ground reads ground, only one thats hot is the tach wire in the ig switch. Shit! With the burn marks inside the switch case I am guessing it is the switch if not the only thing left is the switch box 250 bucks! I will start with the 30 dollar switch. I know at this point we should take it in, but with my step daughter getting married money is a little tight... I can't get back down till the end of June now. Needless to say frustration has set in!
pics under the Stator post
